
However the 3rd Platoon of the 697th Engineer Company
(Pipeline) did perform missions at Kunsan and Osan, Korea during the Viet Nam
Conflict time frame (1968).
Below is the After Action Report from those missions
as written by 1LT John A. Stockman, 3rd Platoon Leader. We are still trying to
establish names of the enlisted personnel that accompanied 1LT Stockman from the
hot wet rice patties of Thailand to the freezing wet rice patties of Korea.
THCON-D |
24 May 1968 |
Commanding
0fficer
44th Engr Gp (Const)
ATTN: THCON-OP
APO 96233
1. On
or about 3 February 1968 the 697th Engineer Company (Pipeline) was alerted to
prepare a full TO&E platoon to leave the theater of operation. A new
platoon of forty-three (43) enlisted men and one (1) officer was formed. The
personnel making up the platoon were men of sixty (60) days or more service
left in Thailand. To fill a full strength platoon, it was necessary to take men
from various slots in the company leaving a critical shortage of manpower in
the company.
a. Around the clock operation was initiated to process
vehicles, tools, and men. On or about 28 February 1968, a message was received
stating that all TO&E equipment minus vehicles would be taken.
b. On 4 March 1968 two (2) Non-commissioned Officers and
three (3) Enlisted Men departed from Korat Air Force base, as the advance
party. The remaining personnel of thirty-eight (38) Enlisted Men and one (1)
Officer departed from Korat Air Force Base on 6 March 1968 and arrived at
Kunsan Air Force Base, Korea at 0200 hours 7 March 1968. After approximately
thirty (30) minutes of waiting, 44th Engineer Group (Construction), Executive
Officer arrived to receive the platoon. The men were then taken to a 'Tent
Village."
(1) The Medium GP Tent with Army cots and sleeping bags were
utilized for the Enlisted Men's billeting for the duration of the Kunsan
Project.
(2) Housing was critical on this base due to the rapid
build-up throughout Korea at this period of time.
2.
The mission of the Kunsan Project was the installation of approximately seven
(7) miles (36,960 feet) of six (6) inch coupled, light-weight victaulic pipe
and approximately 4,600 feet of heavy duty buried, welded pipe.
a.
Much concern and interest was placed on this project. The immediate build-up of
U. S. Forces in Korea because of increased North Korean threats resulted in a
critical problem of rapid jet petroleum transportation from the receiving
terminal to the U. S. Air Base fuel storage area.
b.
The receiving terminal, approximately eight (8) miles from the U. S. Air Base,
received the fuel by ship. From the terminal the jet petroleum would be pumped
into railroad tankers and shipped to various U.S. Air Bases in the immediate
area. The increase in fuel demands could not be filled under their present
installation. A six (6) inch pipeline to Kunsan Air Base was constructed to alleviate the time
necessary to rail fuel into the U.S. Air Base.
3.
The immediate change from a tropical climate to a frigid climate imposed health
problems to the troops. The metabolism of the men was adjusted to adverse heat
conditions. The men made a rapid relocation where there was a temperature
differential as great as seventy (70) degrees at various times. Greater than 70
per cent of the troops at one time or another went on sick call for either sore
throats or severe head colds, resulting in a high loss of man power.
a.
The winter issue of clothing was made the following day of arrival in Kunsan.
(1)
Issue consisted of: One (1) field jacket, without the liner; and two (2) sets
of OG shirts and pants.
(2)
Numerous troops requested woolen underwear, however, S4 of the 44th Bn, stated
that they were not obtainable at the present time. Several men purchased their
own woolen underwear through the local base exchange.
b.
A request for work gloves and rubber boots was also forwarded to the 44th Bn's
S4.
(1)
Approximately two (2) weeks, from the date of the request, the men received the
work gloves.
(2)
The rubber boots were not obtainable.
a.
Rubber boots were requested because several of areas of the route of the
pipeline were in rice fields that were flooded at times.
b.
Troops on various occasions had to work in the icy water resulting in wet feet,
which attributed to the high rate of sore throats and head colds.
4.
The job directive for the eight (8) mile pipeline, Kunsan, was assigned to
Company C of the 44th Engr Const Bn, Headquarters located at Camp Carroll,
Waegon, Korea. The third platoon of the 697th Engineer Company (Pipeline),
Headquarters located at Camp USARTHAI, Korat, Thailand, was attached to Company
C for administrative and operational control. Company C furnished all the
vehicles for the project.
a.
The vehicles consisted of one (1) jeep (for the use of the 697th platoon leader),
three (3) five-ton dump trucks (for each of the squads in the 697th's third
platoon), and one (1) lowbed and tractor for the transportation of the pipe to
the installation site.
b.
Adequate vehicles were available to the 697th for the project.
c.
The 44th furnished one (1) platoon for the project. The 44th platoon was
utilized in assisting in the installation of culverts for road crossings; the
coating of the welded pipe with tar; and the digging of the trench for the
buried pipeline.
d.
Company C also installed approximately one-and-a-half (1 1/2) miles of tactical
coupled pipe, receiving technical assistance from the 697th.
5.
The 697th pipeline Company was called upon to send a full strength platoon from
Thailand to Korea to assist in what was considered a highly specialized job,
however, it is felt that the attached command and higher headquarters did not
fully realize that the 697th platoon was quite familiar from past experience
with the installation of tactical pipe. At the commencement of the project the
44th Bn caused unnecessary chaos by not working with the pipeline officer and
giving him credit that he had experienced knowledge in this type of work. The
project officer was a 2LT from Company C who had never seen the installation of
tactical pipe prior to this day. The Company C project officer failed to
realize what was critical in the installation phase, several misunderstanding
between the 697th platoon leader and the pipeline project officer resulted. The
project officer and his sergeant would reassign various jobs to the pipeline
platoon after the 697th platoon leader would have them assigned to a specific
detail, this caused much confusion among the men.
a. Daily
operation meeting did not eliminate this problem.
b. Besides the confusion between the 697th platoon leader and
the Company C project officer, the Battalion Executive Officer and Company C
Commander stayed on the project the majority of the time, resulting in four (4)
officers trying to run the job. However, as the job progressed the Battalion
Executive began to realize that the 697th platoon leader and platoon was
capable of doing the job, in turn, the Executive Officer began to respect any
recommendations made by the 697th platoon leader.
(1)
However, approximately one (1) week before dead line day the 697th Platoon
leader felt that the project was getting too disorganized because of over
supervision.
(2)
The 697th platoon leader then told the Battalion Executive Officer that the
project would run and progress much better if there was not over supervision.
The battalion executive officer accepted the 697th platoon leader's complaint
and he had the Company C Commander sent back to his headquarters. He also put
the 697th platoon leader in charge of the project, also he himself went back to
his headquarters.
c.
The critical need for this pipeline is the reason for the problems of over
supervision. 44th was in continued harassment to get the pipeline completed.
Misunderstanding did not result from poor officers. 44th has the highest
caliber of officers. The problem was that this was considered one of the
"hottest" construction projects going on in Korea at this time, as a
result, everybody wanted to help.
6.
There were several obstacles incorporated into the installation of the tactical
coupled phase that hampered operations.
a.
After approximately a thousand feet of pipe had been installed, including two
(2) buried road crossing, word was received from Eighth Army's G3 that no
curves with radii less than 48 inches would be used. The reason was that they
wanted to pump a wiper plug through the eight (8) mile line after it would be completed.
As a result, all pipe would have to be heated and bent. A pipebending machine
was designed, incorporating a twenty-ton jack and built by the 697th. The
apparatus was quite effective, however, it was a slow process because of the
numerous road curves, ox cart trails or road crossing in which eighteen (18)
inch culverts were installed with the pipe running through the culverts. As a
result, the initial thousand feet that was installed, did not incorporate these
features therefore, had to be made several modifications.
b.
The design of the pipeline called for supports spaced every joint of the pipe.
Wooden supports were made, however, after two miles of supports were installed
the local Natives found that the wooded supports was the answer to their fuel
shortage. This operation was eliminated.
c.
Indecisions on the route location caused several wasted man hours.
(1)
The first two thousand feet of pipe installed on the Air Base had to be moved
from one side of the road to the other because it was not 100 feet away from a
Nitrogen Plant.
(2)
Approximately one (1) mile of pipe on a levee had to be located on the opposite
side of the road because some VIP liked it better on the other side.
(3)
A thousand feet of pipe going through a rice field had to be moved because some
rice farmer complained to Eighth Army, which stipulated that the easement had
not been checked, as shown by the drawings.
7.
The 4,600 feet of welded buried pipe, also introduced problems.
a.
The digging of the trench was the major obstacle. The trace for the buried pipe
was the cutting of a three foot trench on the side of a rock road going through
a heavily populated village. The reason for this route is because to the East
of the road was mountainous terrain while to the West of the road was the
Yellow Sea. The pipe had to be buried because of the hazardous of a tactical
line in such a populated area. A 750 Barber Greene Entrenching machine was
utilized, however, the encountering of rock caused several mechanical break
downs. A ten ton backhoe was then brought to the project, however, the backhoe
outcrops (?); such areas had to be done with jack hammers. One area,
approximately 300 feet, was of solid granite as a result, pipeline was welded
and installed above ground.
b.
The welded buried portion of the pipeline had to be coated with tar, wrapped,
and then recoated. Such an operation should have the proper equipment, which
the pipeline platoon was not equipped. The 697th coated approximately 1000 feet
then the remaining pipe was coated by Company C personnel. The results of the
coating was of poor quality, but this was expected because of the means
available to do the coating.
c.
Problems with the local natives were encountered. Large crowds of native
spectators would gather around the construction, exposing themselves to
construction equipment. The working personnel were in constant fear of hurting
someone accidentally, however, there was no incident. Vehicular traffic through
the area of entrenching caused several traffic jams. This became such a problem
that the digging operations was done only between 2300 hours to 0700 hours,
hours in which the least traffic was encountered.
d.
Lack of highly experienced welders presented an area of problems. Although, the
697th and 44th's Company C had several Army trained welders, the welders were
not sufficiently qualified for pipeline welding. Only two men from the 697th
were qualified for pipe welding. Toward the latter part of the welded portion
of the pipeline, Company C did receive a qualified pipe welder that was also
utilized. The welders were very critical and they were over worked. There were
times when they actually put in sixteen (16) hours a day of steady welding,
which is too much of a strain on them to maintain quality welds. Time was lost
due to break down in welders. The 697th brought only one welding machine, the
44th furnished one also. However, there was mechanical breakdowns that deemed
it necessary to borrow welding machines from the Air Force.
8. Another
perplexity that originated on the buried welded was the breaking of several
water lines. Before any digging started the 697th platoon leader requested
information on the probability of buried lines. Check was supposed to have been
made with a negative report. After two thousand feet of digging, the ten ton
backhoe ruptured a 13 inch cast iron water main serving the town of Kunsan.
Eighteen hours was lost repairing this leak. Concern then aroused over this
line. Investigation through several of the local natives, revealed that the
pipeline was buried four (4) feet and crossed the road five times in attempts
to dodge granite outcrops. Instead of waiting on a complete check of the
location of the water pipe, Company C had the 697th move a thousand feet of
welded pipe to the opposite side of the road, however, after it was learned
that the pipeline zigzagged across the road, 44th realized that the opposite
side of the road did not offer a solution. The thousand feet was then moved
back to other aide. Since the waterline was buried at four (4) feet, 44th had
the new line brought up to a depth of two (2) feet. Besides the 13 inch water
main, several small one inch lines were damaged and had to be replaced.
9. On
27 March 1968 the complete pipeline was ready for water testing. Water was to
be pumped from a 250 BBL water tank at the Army Receiving terminal to the Air
Force Base. The Army Receiving terminal had four (4) inch centrifugal pumps.
Two pumps were estimated to be needed to pump the eight (8) miles. The capacity
of the pipeline was approximately 70,000 gallons of water. The water source to
the water tower, at the Army terminal, was connected to the Kunsan waterman in
which the water was only turned on for eight (8) hours a day. The pipeline was
disconnected at one (1) mile increments where it was flushed and then pressured
up to 300 psi. Two (2) miles were tested in this manner, however, time was lost
waiting for the tank to fill up, also only one pump was operational and
difficulty in building up the pressure was encountered. About half way long the
line the Air Force, had their water station. A request to the Air Force to use
their pump station was approved. A line to their pump house, 100 feet away was
installed. Four (4) miles of line at a time was flushed and tested to 300 psi.
Delay in water testing facilities began to throw the project behind schedule by
two days. Request to work all night testing the line was made by the 44th En.
The 697th platoon leader asked that testing and repair of leaks be done during
the hours of light so that adequate light would be available to correct the
leaks, also because the repair of leaks was over an eight (8) mile span with
various areas in rice fields, thus making the use of generators a problem to
use. Higher command insisted to work all night. Flashlights were used. Before
the line was completely satisfactory, as to leaks, the order to start pumping
fuel was given. No coordination to an inspection while under water test, was
made between the POL personnel, that would be operating the facility, and the
construction outfit.
10. Upon
completion of the project there was confusion on what the 697th was to do. The
697th was under the impression that they were to return to their home unit in
Thailand. A request for airlift was sent to the Eighth Army by the platoon
leader. A reply that they were to stay in Korea for the full period of sixty
(60) days was returned by Eighth Army.
11. On
4 April 1968 the 44th Battalion Commander called the 697th platoon leader and
told him to report to the Second Group Commander located at Kimpo. The Second
Group Commander briefed the 697th officer on what little he knew of a two (2)
mile pipeline that was to be installed at the Osan Air Base. There was still
confusion on who was responsible for arranging for the transportation of the
697th to the new job location. Second Group stated that they did not have any
orders attaching the 697th to them. Therefore, they felt that the 44th Bn was
responsible for arranging for transportation. Upon return to Kunsan 44th was
under the impression that arrangements were being made by Second Group.
Transportation was then arranged by 44th En. Three days prior to the unit
moving to Osan to be attached to the Company B, 802d Bn, an advance party of
two Sergeants was sent to make all the necessary arrangements. The 697th
platoon arrived at a Korean train station twelve miles from Osan. The 802d met
the 697th platoon and transported the men to tents that had been set up for
them. The 697th platoon leader then reported to the Company B Commander,
however, the Commanding Officer could not see the 697th officer until the
following morning because the Commanding Officer stated that he was tied up at
the time. A request to the operations officer for the men to have
transportation to pick up their bedding and to take them to chow was made.
However, the request was denied on the grounds that it was after 1700 hours,
697th was told that the linen issue was only three blocks away and they could
walk. However, Company B failed to realize that this was the first time that
the unit was on base and was not familiar with the location of the facilities.
The 697th platoon leader questioned his two sergeants that was sent as the
advance party, as to why this had not been set up prior to the platoon's
arrival, the reply was that attempts were made to set it up, but Company B
personnel did not have the linen to issue. The following morning, 13 April
1968, the 697th officer discussed the project with Company B Commander. The
Commanding Officer obviously had not been informed of the platoon's needs,
which had been set up with Second Group's S3, because they were under the
impression that the platoon had its own vehicles. The Company B Commanding
Officer told the 697th officer to see if he could borrow vehicles from the Air
Force, also to check with PRIME BEEF of the Air Force on what the job was
about.
12. PRIME
BEEF briefed the 697th officer of the project and stated that material left
from the Kunsan project would be utilized until their supplies arrived. Eighth
Army had passed down to Second Group that they were to arrange for the
transportation of the remaining pipe from Kunsan to Osan, however, action did
not seem to be taken place, therefore the Air Force sent a lowbed that night to
Kunsan to pick up a load of pipe so that the pipeline platoon could get
started, while the rest of the pipe would be transported by rail, also the
PRIME BEEF Commander assigned two Master Sergeants to assist the 697th in
arranging the rail transportation for the pipe because Second Group had not
made the arrangements prior for the railcars.
13. Transportation
was major problem at the Osan project. Company B was only able to supply one 2
1/2 ton truck. This obstacle hampered construction because three sections were
working on various areas in the two mile stretch. Eighth Army's G3 became quite
concerned over this problem and told 802d Bn that the pipeline was top priority
and that the pipeline would get whatever support necessary. However, poor
support still resulted and a complaint was made to G3 by the 697th platoon
leader, after that, the 697th had no more problems with transportation.
14. Available
material hindered the installation. There were no 90's, 45's, or Tee's
available initially and therefore had to be constructed, however, at the latter
part of the project, after they had already been fabricated by the 697th
welder, the material came in. The supply of couplins became exhausted prior to
approximately two thousand feet to completing the project. Several days were
lost waiting for an airlift of couplings. The 697th was scheduled to be back in
Thailand not later than 4 May 1968. Concern as to how much work would be left
unfinished since time was running out developed. Outlet fittings were still
lacking therefore, testing of the pipeline was initiated. Water under 150 psi
was utilized for testing. The pipeline was inspected by the 802d Bn Commander,
PRIME BEEF Project Officer, and the Air Force POL Officers; the water test was
approved by all parties.
15. All
necessary information for return airlift was submitted approximately two (2)
weeks in advance. Two days before the platoon was to be airlifted, the 802d Bn,
Second Group, and Eighth Army transportation started calling the 697th platoon
leader, they were confused on who was to request the airlift. A complaint was
made to G3. An investigation revealed that the paper work had never gone down
the line. G3 then had to make a verbal request.
16. On
3 May 1968, one of the two C130's departed at 0900 hours with the third platoon
of the 697th and arrived in Korat, Thailand 0700 hours, 3 May 1968. The second
C130 with one sergeant and two EM arrived with the platoon's equipment on 5 May
1968.
17. In
conclusion, the overall major problem with the Kunsan project was over
supervision. The 697th platoon leader should have had more control in the
construction operation. The Osan project. showed no support administratively
and equipment wise until formal complaints were made to G3 of Eighth Army.
|
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John A. Stockman |
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|
1LT, CE |
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|
Platoon Leader |